Recent Developments in Plugging of Steam Generator Tubes

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S. Buhay
R.C. Abucay

Abstract

Mechanical Plugging capability has been developed for Bruce Nuclear Generating Station (BNGS) steam generator (SG) tubes and Darlington Nuclear Generating Station (DNGS) SG tubes and tubesheet holes. The plug concept was a modified ABB/Combustion Engineering Inconel 690 plug with a nickel band, rolled into the tube or tubesheet hole from the primary side of the tubesheet. The qualification program included analytical justification of the plug body and experimental testing to verify the leak tightness of the rolled joint under conditions which meet or exceed all service or design requirements. Tools and procedures were developed and tested for manual and remote/robotic installation and removal of the mechanical plugs. Additionally, tools and procedures were developed to plug tubeshubesheet holes at DNGS in the event the steam generator is recalled to service to act as a heat sink. A crew of Ontario Hydro personnel were trained and qualified for the installation of mechanical plugs for permanent and recall applications. During the DNGS Unit 4 spring 1995 outage, 6 tubes were plugged and the "Recall Plugging Capability" was deployed and ready for use during a primary side SG tube removal. The mechanical plugs were installed manually with a typical 3 minute/plug in-bowl duration time with an average radiation dose of 12.5 mrem per plug. This compares favourably with manual plug welding during the same outage in the same SG bowl at approximately 15-30 minutes/plug in-bowl duration with an average radiation dose of 117mrem/plug.

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