Assessment of Causes for Degrading Fuel Performance at Darlington NGS
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Abstract
Fuel performance at the Darlington nuclear generating station has historically been excellent. Until recently, the majority of these few fuel defects have been attributed to fretting by heat transport system debris. The minority have been linked to manufacturing issues. Recently, Darlington has experienced an increase in the number of fuel defects. Although the defect rate remains low with respect to industry standards, this defect experience is considered to be unacceptable given current industry expectations and the OPG zero defect policy. Nine fuel defects have been discharged since 2007 from the four Darlington reactors. This represents a fuel defect rate of just 0.35 defects per year per reactor. At the time of this writing three additional defects are suspected to be in core. Although a definitive defect cause has yet to be identified, these fuel performance issues appear to be due to the coincidental degradation of manufacturing and operational factors, thereby decreasing the margins to fuel failure due to fuelling power ramps. All of the confirmed defected bundles have been long bundles and all experienced a relatively high power ramp when shifted from Position 2 to Position 6.High bundle uranium masses and low internal clearances are thought to be strongly contributing factors. Bundle burnups at the time of the power ramps were low and these bundles were not identified by existing power ramp defect predictive tools. Our assessment has resulted in a number of recommendations which are designed to mitigate these adverse conditions by restoring the margins to power ramp failures. These recommendations impact broadly across a number of organizations including reactor physics, fuel design, fuel manufacturing, reactor design, inspections and PIE.
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